Some Junk We Found
Cracked and VERY worn rotor housing.
Busted coolant seal. This explains the coolant I had in my oil, but how did the gas get there...?
Port job done with a chisel! Oh, Did I mention this is the Primary Plate! Not sure what the hell this is supposed to do...
The sad thing is, this motor supposedly had 5K on a rebuild. The engine had oil and grease caked on it. There were multiple stripped bolts, electrical tape on the Turbo inlet duct, and JB Weld EVERYWHERE! Before it blew, the engine was compression tested at about 65-70 psi.
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